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updated: 1/31/2012 2:07 PM

Byron reactor shutdown blamed on bad insulator

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  • Steam rises from one of the two cooling towers Monday at the Byron nuclear generating station in Ogle County, Ill. A loss of power coming into the plant caused one of the reactors to automatically shutdown Monday morning.

    Steam rises from one of the two cooling towers Monday at the Byron nuclear generating station in Ogle County, Ill. A loss of power coming into the plant caused one of the reactors to automatically shutdown Monday morning.

Associated Press

A failed electrical insulator in a switchyard was to blame for the power failure that caused one of Exelon Energy's nuclear reactors in northern Illinois to shut down, company officials said Tuesday.

Officials hoped to replace the part by the end of the day. The company would then begin preparing to re-start the Unit 2 reactor at the Byron Generating Station about 95 miles northwest of Chicago, though it remained unclear how soon it could return to service, spokesman Paul Dempsey said.

The insulator, a piece of protective equipment that helps regulate the flow of electricity in the plant's switchyard, failed Monday morning and fell off of the metal structure to which it was attached. That interrupted power and caused the reactor to shut down automatically as a precaution.

It was not immediately clear what caused the insulator to fail, but the part will be sent to a lab for analysis, Dempsey said.

During the shut-down, steam was released to cool the reactor, but was being vented from the part of the plant where turbines produce electricity, not from within the nuclear reactor itself, officials said. The steam contains low levels of tritium, a radioactive form of hydrogen, but federal and plant officials insisted the levels were safe for workers and the public.

The U.S. Nuclear Regulatory Commission declared the incident an "unusual event," the lowest of four levels of emergency. Commission officials also said the release of tritium was expected.

NRC spokeswoman Viktoria Mitlyng said officials can't yet calculate how much tritium was released. They know the amounts were small because monitors around the plant didn't show increased levels of radiation, she said.

Tritium molecules are so microscopic that small amounts are able to pass from radioactive steam that originates in the reactor through tubing and into the water used to cool turbines and other equipment outside the reactor, Mitlyng said. The steam that was being released was coming from the turbine side.

Tritium is relatively short-lived and penetrates the body weakly through the air compared to other radioactive contaminants. It can cause cell damage if it enters the body, but the amounts released from the Byron station under normal operating conditions and within the steam that's being vented now is not a health concern, said David Lochbaum, a nuclear engineer and director of the nuclear safety project for the Union of Concerned Scientists.

Releasing steam helps "take away some of that energy still being produced by nuclear reaction but that doesn't have anywhere to go now," that the turbines are shut down, Mitlyng said. Even though the turbine is not producing electricity, she said, "you still need to cool the equipment."

Candace Humphrey, Ogle County's emergency management coordinator, said county officials were notified of the incident as soon as it happened and that public safety was never in danger.

"It was standard procedure that they would notify county officials," she said. "There is always concern. But, it never crossed my mind that there was any danger to the people of Ogle County."

Diesel generators were supplying the reactor with electricity, though it hasn't been generating power during the investigation. Another reactor at the plant was operating normally.

In March 2008, federal officials said they were investigating a problem with electrical transformers at the plant after outside power to a unit was interrupted.

In an unrelated issue last April, the commission said it was conducting special inspections of backup water pumps at the Byron and Braidwood generating stations after the agency's inspectors raised concerns about whether the pumps would be able to cool the reactors if the normal system wasn't working. The plants' operator, Exelon Corp., initially said the pumps would work but later concluded they wouldn't.

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